Hi guys,
I took my bike from the mechanic and had the time to write about the progress. Here's the bike after the 6 hours trip on a trailer back home:
The compression of the cylinders is still high, about 13 and I hope it'll drop down to the specified 10, otherwise it's possible to have to repalce the piston rings.
From the moment I bought the bike the throttle wasn't moving freely. I checked the mechanism:
The lubrication didn't help but revealed the problem - throttle wire was bad:
It was fixed by a local company - replaced the cable and bottom half of the cable housing:
Exept the gray (comming from burning oil) smoke, I supposed a bit reacher than usual mixture. The spare airflow metter I had was oppened so i tighten 2 teeth on the spring. This gave bit more tension than my original airflow meter - one tooth is enough to make them equal, and I put one to respect the age
. I put the spare one in the air filter case. I'll correct precisely the mixture later.
Then I installed the airflow box:
The ECU (brain):
The button controlling lights on the right console wasn't moving freely so I gently put the console appart. There are a lot of small parts, so You should be careful not to loose something:
Then, I reassemble some of the plastics to test the bike:
Aftermarket screen, I bought several months ago:
Spark plugs cover:
The bike run with the borrowed Hall sensors and I did 2km test ride. The bike was running smoothly, so I was happy.
I decided to finally test the blamed Hall sensors::
Here is the two sensors on the plate:
After some test I saw that the sensors were givving correct signals below voltage 10-11V:
After that, one of them is giving 1V signal no matter if it's closed or open. Here You can see that it returns only 1V, despite the fact that it should return the supplied voltage ~12,2V:
This one is working correctly:
Placing a metal oblect should result in no signal:
The defected one is again returning that bad signal ~1V:
This may result in two of the spark plugs not to be working at all.
Yesterday I had the chance of having sunny and relatively warm weather (5C), so I rode the bike still not fully dressed, about 40km. It was running smooth, and the smoke has gone. Only a bit when revving hard, probably still a bit rich mixture. Here is some short video of that bike autumn ride:
https://www.youtube.com/watch?v=uH7KeFaQBBoThis is for now.
Thanks everyone! I'll post some information when I complete the restoration, or if some problem comes up again.