1 outputshaft? Sat Apr 05, 2014 4:02 am
k-rider
Life time member
Well,, here is a question that i hopped i did not have to ask
this winter i did a renovation of the outputshaft in my 84 engine.
the reason is that it had a very loud knocking sound , especially when cold.
so i thougt that was it.
It turned out to be a missing fibre washer behind the clutch basket , and also the ball bearing on the outputshaft was rotating in the housing.
had a spare engine so i could pick the best of the two ,lower enginecase from the spare and the outputshaft from the faulty one was surprisingly the best of the two ,no play in the rivets at all.
ordered new bearings for the outputshaft and alternator drive also new o-rings all way round.
a couple of weeks ago i got it assembled an fired up ,at first i was thrilled because the k nocking sound was completely gone .
well at least for a few moments.
now there is a higher pitched knocking sound ,only between 1300-2100 rpm.
at first i thougt it was something in the alternator area, so took that apart and drove the bike without it ,the sound is still there and didnt change at all.
i did a stetoscope investigation with a screwdriver and that , to my surprise points directly to the waterpump, it sounds like someone is using a litlle hammer on the inside of the cover.
having a spare i swapped it with that, still no change.
put in a thicker oil yesterday 15/50 instead of 5/40.
And that may have made a slight change , but the noise is still there
now im all out off good ideas , can someone come up with anythinng.
hoping that im not having to take it all apart again.
best regards
k-rider
this winter i did a renovation of the outputshaft in my 84 engine.
the reason is that it had a very loud knocking sound , especially when cold.
so i thougt that was it.
It turned out to be a missing fibre washer behind the clutch basket , and also the ball bearing on the outputshaft was rotating in the housing.
had a spare engine so i could pick the best of the two ,lower enginecase from the spare and the outputshaft from the faulty one was surprisingly the best of the two ,no play in the rivets at all.
ordered new bearings for the outputshaft and alternator drive also new o-rings all way round.
a couple of weeks ago i got it assembled an fired up ,at first i was thrilled because the k nocking sound was completely gone .
well at least for a few moments.
now there is a higher pitched knocking sound ,only between 1300-2100 rpm.
at first i thougt it was something in the alternator area, so took that apart and drove the bike without it ,the sound is still there and didnt change at all.
i did a stetoscope investigation with a screwdriver and that , to my surprise points directly to the waterpump, it sounds like someone is using a litlle hammer on the inside of the cover.
having a spare i swapped it with that, still no change.
put in a thicker oil yesterday 15/50 instead of 5/40.
And that may have made a slight change , but the noise is still there
now im all out off good ideas , can someone come up with anythinng.
hoping that im not having to take it all apart again.
best regards
k-rider
Last edited by k-rider on Sat Apr 05, 2014 6:19 am; edited 1 time in total
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k100rs 1983 -o:
Shinny black ,exaust from a 16valve ,engine from a 1990 K100 lt,fd ratio :32/11
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