RicK G wrote:That 32 amp alternator is an up grade from a lower amperage alternator and is fairly much on its limit. Once it gets past 22-23 amps it starts to get voltage drop off and lights get a bit dimmer and charging becomes eratic at best.
Thanks Rick - I had no idea that the regulator was that poor. I'm used to dealing with systems that give full voltage right up until the last three or four amps.
Olaf - my Cali 1100ie fuel pump is rated at 4 amps draw, so as it's pushing the same pressure as the K100 pump I'd guess it's a safe bet that the K100 pump draws the same? For the fuel injectors, (as Rick reminded me in another thread), each one fires twice per cycle so the
average load is quite low. In addition, if you can fire them with a 9volt PP3 battery for cleaning they can't be drawing much current. Still, it would be nice to know just what their current consumption is.
While we're at it, can anyone tell me why some alternators as marked as 32A and other, seemingly identical, ones are marked as 33A? Just a part number change?
Touchwoodsden - I've just had a dig through my garage storage area and turned up a spare 50amp alternator. IIRC that one cost me a pound-per-amp; it's yours for that plus postage. PM me if you're interested.
Conversion from 50amp to 60amp; this was my experience so YMMV. I got a cheap K1200 alternator off ebay for the donor. The drive mechanisms came off first (belt drive on the 60amp, monkey-nuts on the 50amp). I took the regulators off and then removed the stator and armature from both alternators. The stator comes off by just removing the three screws that holds the alternator together. You may need a mallet to separate the casings because of corrosion - I did. Ditto to drive the armature out of the front casings. A bit of heat helps with the armature and IIRC, there's a plate holding the front bearing in. I put the 60amp armature into the 50amp front casing (the bearings are the same) and then bolted up the 60amp stator. This revealed the only problem during the whole process - doing this makes the bearings bind.
To fix it, I separated the casings again, pushed the three bolts through the rear casing and dropped a washer over each bolt before bolting the cases back together again. The washer acts as a spacer. I also put a small smear of copper grease on the back of the rear bearing as a telltale. The armature now spun freely, so I dismantled the assembly for a third time to check my makeshift telltale. I found a tiny amount of spread, just about what I'd expect from what was effectively a very crude check, so the assembly went back together for the last time and the monkey-nut drive was bolted on.
It's been two years since I did this and it's behaved perfectly. There's about 15mm clearance between the back of the alternator and the front of the battery.